ZeXx86 wrote:
Thank you very much!
It is sad we can't test it internally at the moment. But with your help it should be fixed soon.
Here is another one to test:
http://spirit-system.com/dl/fw/test/spi ... -test6.binI believe that there is a problem with Failsafe at the moment.
If so (and previous firmware does not help) then this firmware will fix it.
http://spirit-system.com/dl/fw/test/spi ... -test7.binIt is hard to determine where could be the issue, so it can't be fixed by first try
Ok,
I have done the following..
Powered on Heli, & TX to retest.
Save results as before with test5
Then
Updated firmware to test6.
Power cycled heli/restarted software
Powered off TX.
The failsafe values were shown on the diag screen.
Clicking on log caused the tail servo to move as before.
Then power cycled Heli,
Updated to test7.
Power cycled heli/restarted software
Powered off TX
The previous values were displayed (ie not failsafe)
Clicking on open log did not cause tail servo to move.
Thought I would repeat the test.
Then power cycled Heli,
Updated back to test6.
Power cycled heli/restarted software
Powered off TX.
Failsafes displayed, and no tail movement when opening log files.
Thoughts?
Cheers,
Yak.