ZeXx86 wrote:
Hello,
thank you for your message.
First from all I recommend to verify following:
1. Start the Spirit Settings and open the Servos tab
2. Click at the Subtrim (tuning)
3. All servo arms should be at the center at this moment - as close as possible to check with eye - usually it is hard to measure with other tools. If you are not sure, then please take a photos of the servos in this moment.
4. Check if swashplate is really levelled at the same time - still in the Subtrim (tuning) menu.
5. Check if there is 0° between main blades - still in the Subtrim (tuning) menu.
All these steps must be checked and configured it is really good - all at the same time, because all Altitude related features are dependent on precise configuration of the swashplate/blades.
Hi Tomas,
as you advised i checked the settings in the subtrim menu. With engaged subtrim Swashplate is leveled. 0 degrees between the blades and all servo arms at the center.
Please see the pictures
Attachment:
File comment: Swashplate leveled
-5312519987468026404_121.jpg [ 95.43 KiB | Viewed 285 times ]
Attachment:
File comment: Blades at 0 degree on pitch stick in the middle
-5312519987468026401_121.jpg [ 118.97 KiB | Viewed 285 times ]
Today i did another check flight. It's still the same problem. Position hold is ok. Auto Landing is way to fast down movement. RTH does not reach the return height as set in the settings tab. Should be 8 m. Rapid down movement by switching RTH.
Pitch still 2/3 of the stick movement necessary for hovering.
I try to upload my film with a helmet cam. It's not best quality but i hope you can see the problem.
Upload not possible because of spirit system error 500.
Best regards
Markus