Hi guys,
could someone please help with this problem?
A bit background -
i put my logo 550 in the ground due to a Bec going dead on me... not a bad crash at all really as i managed to get it flipped over and almost level just before i lost full control. I fixed the model and at the same time noticed a new firmware for the Spirit unit was available and so flashed and re-setup the unit ready for its test hover. All straight forward stuff thats been done many many times. Test hovered the heli and it basically front flipped from the second it left the ground. Only damage was a slight crack in the blades.
Got bored and had other projects on the go and so the heli sat in a corner for a couple month. Eventually come round to looking at it again. Flashed Spirit with another firmware bringing up to the present version. Reset the unit and done a full setup again. When bench testing i found the following issue. The sensors are all correcting in the right direction but the swash doesnt react like it should as soon as throttle (rpm on the head) is received. Without throttle everything seems normal. As you can see in the following video there are no vibrations either. One thing that i noticed is that when the unit initializes the swash does not go straight up and down. I can also confirm that the rescue mode switch is not engadged (check direction in the software) Anyone have any ideas whats going on? Im thinking the unit is faulty. Ive set these up many times before and they normally fly great straight from the first hover. Im using the mikado logo 550 preset.
https://youtu.be/6cf0WFtobBk