Hi all
Would love your collective help in helping me fine tune my governor so I get the best performance out of my Goblin Black Thunder. I've installed jLog and connected to my HW130a V4 and have managed to get detailed telemetry data so hopefully someone can help me fine tune it or tell me if its as good as it can get
I've been performing some sloppy tic tocs as can be seen in the telemetry screen below:
Attachment:
Tic Toc Full.jpg [ 760.35 KiB | Viewed 679 times ]
If I zoom in you can see a bit more detail:
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Tic Toc.jpg [ 740.06 KiB | Viewed 679 times ]
Lets take a "Tic" cycle at 8:50. As I am unloading the head, the gov drops to 89% throttle. When I reach inverted and punch the collective it jumps to 97% throttle. Also pushing up the current to 86.9A from circa 24 amps hover current and 26A when I was flipping it backwards.
At that stage I notice the RPM dropping from a 21160(motor rpm) / 1977 rotor RPM to 20760 motor/1940 rotor before jumping back up to 21730 / 2030 rpm. At that point throttle starts to drop from 97% back to normal 89%.
So Im experiencing about a 30-50 head RPM drop followed by a 100rpm "correction.
Also in the below pitch pump:
Attachment:
pitch pump full.jpg [ 762.81 KiB | Viewed 679 times ]
I start from 21797/2037 head RPM. Then drops to 20283/1895 rpm. I can see the throttle increasing when the RPM are at 21419/2001 (i.e. after it has dropped by 30rpm or so but that could just be normal fluctuation of the rotor head) from a 82% linearly to 91.9% at the lowest point in the RPM - 20270/1894. It then gradually reduces as the headspeed rises to 22563/2108 rpm but it does not go down quick enough as the RPM increase hence the overshoot. So it ramps up quick (or slow??) enough to loose about 140rpm then overshoots by about 70rpm or so.
My settings are:
Response: 6
Holding performance: 4
Target RPM: 2000 (or so)
Should I increase governor response and reduce holding performance? I havent done any long load tests so havent really tested the holding performance but during the tic tocs it did not loose on average any headspeed.