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PostPosted: Mon 06. Sep 2021 19:50:13 
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Joined: Sun 05. Sep 2021 10:18:09
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Hi, I have a problem with this gyro and Goblin RAW, when the tail spins disadvantage torque (clockwise) it swings very very strong, I tried to decrease the tail sensitivity but the problem persist.
Thanks so much


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PostPosted: Thu 09. Sep 2021 20:14:37 
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Hi,

can you please share your settings file?
What is your tail servo?

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PostPosted: Fri 10. Sep 2021 20:08:43 
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ZeXx86 wrote:
Hi,

can you please share your settings file?
What is your tail servo?


The tail servo is KST MS805, ESC is the Hobbywing 200A v4.1 setted by default.
at 2000 rpm ok 34 rud sensitivity
at 2300 rpm is ok 12-10 rud sensitivity
is it normal?
Thanks so much.


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PostPosted: Sun 03. Oct 2021 19:22:15 
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Joined: Sun 05. Sep 2021 10:18:09
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Thanks for the support (non-existent) I solved alone!
vellodoro wrote:
ZeXx86 wrote:
Hi,

can you please share your settings file?
What is your tail servo?


The tail servo is KST MS805, ESC is the Hobbywing 200A v4.1 setted by default.
at 2000 rpm ok 34 rud sensitivity
at 2300 rpm is ok 12-10 rud sensitivity
is it normal?
Thanks so much.


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PostPosted: Mon 04. Oct 2021 7:58:02 
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Joined: Mon 29. Apr 2013 16:06:44
Posts: 12442
Hello,

your settings looks good. But for this servo changing servo arm to a shorter could help.
Then readjusting rudder end points will be needed.

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PostPosted: Mon 04. Oct 2021 9:37:55 
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Posts: 274
vellodoro wrote:
Thanks for the support (non-existent) I solved alone!

maybe, instead of ranting,
you can share the solution for the benefit of all other forum users :-)


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PostPosted: Mon 04. Oct 2021 16:48:39 
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Joined: Tue 16. Jun 2015 14:37:10
Posts: 156
urgno wrote:
vellodoro wrote:
Thanks for the support (non-existent) I solved alone!

maybe, instead of ranting,
you can share the solution for the benefit of all other forum users :-)


+1. Four posts in and he's up in arms already. Maybe an apology from Tomas for taking less than two days to provide his solution :roll: :)


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PostPosted: Mon 04. Oct 2021 18:31:51 
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Joined: Sun 05. Sep 2021 10:18:09
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I changed the Rudder Common Gain to 1.00 x, although for a Heli 700 it was recommended 1.3 or 1.5 and the problem disappeared. The problem occurred only at 2300 rpm, at 2000 rpm was ok

The FlyBarless Spirit for me is one of the best systems on the market.


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PostPosted: Tue 05. Oct 2021 0:46:03 
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Joined: Tue 16. Jun 2015 14:37:10
Posts: 156
I suspect the crazy headspeed of the RAW may have something to do with it. The Spirit gain multiplier for a 700 size Goblin heli is probably based in a headspeed of 1900/2000


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PostPosted: Tue 05. Oct 2021 8:51:10 
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maybe in the next version there will be a template also for the raw


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