Hi all;
Hoping you can help. I have a Spirit Pro (FW 2.5.1) mounted in my scale Mi-24 Hind, 600 size. Helicopter specs:
- Thunder Tiger Mi-24 Hind Fuselage, approx 14.0 lbs AUW
- Audacity Pantera P6E mechanics (with Stage II clutch)
- Scorpion HKIII 4035 450 Kv motor on 12S (2x 6S) through a Jeti Mezon 90 Opto ESC
- Century Diamond 5 Blade head, 600mm Funkey blades (symetric profile)
- 3 Bladed Miniature Aircraft tail, belt driven through custom intermediate gear box.
- Control is Jeti DS16 through REX12 reciever. Spirit connected via EX Bus.
The helicopter last flew in July with the below settings (in a test rig, not the fuselage), and was pretty stable (changes today in
bold). Today was the maiden flight in the fuselage... Almost ended in disaster. I'm finding that the Spirit is barely stabilizing the helicopter at all. Roll & pitch are very sensitive. Tail is rock solid. Hoping that you all can help.
Video of today's flight is here:
https://youtu.be/v8SZaC90Kh8 I really apologize for the shakiness, it was a GoPro on my head - not the most stable of positions! (Camera wife was at work!)
Spirit Settings:
General:
- Horizontal orientation
- CCPM 120° (reversed)
- Jeti EX Bus
- Flight Style: 4 (was 5 during first part of flight, reduced to 4 after middle landing)
Diagnostic:
- Tail Gyro Gain: Switchable between 56 & 65%
- No Bank switching enabled
Servos
- Cyclic: ProModeler HV BL 1520/333
- Tail: Outrage Torq tail servo (model escapes me) 760/560
Limits:
- Pitch Range: 255 (pitch range limited in radio to -5° / +10°)
- Cyclic Ring: Unchecked
- Aileron/Elevator Range: 180(~14°)
- Rudder end points: L 121 / R 55
Sensor:
- Cyclic Gain: 70 (was 65 during first part of flight, increased to 70 after middle landing)
- Rudder Gain: In Tx, switchable 56 / 65%
- Rudder Common Gain: 1.00x
- Cyclic Rotation Speed: 5
- Rudder Rotation Speed: 5
Stabi:
- Stabilization Mode: Normal, no rescue (Stabilization was only on at the very beginning, after the first attempt to roll over I shut it off from the TX)
- Sticks Priority: 6
- Direction Control Rate: 3 (I may have changed this midway, I don't honestly remember. It might have been 5 prior.)
Advanced:
- Geometry: 104
- Elevator Filter: 2
- Rudder delay: 5
- Revomix: 0
- Cyclic Feed forward: 5
- Rudder dynamic: 4
- Piro Consistency: 160
Advanced -> Expert:
- Stick Deadband: 4
- Elevator Pitchup Compensation: 0
- Cyclic Phase: -56 (there is no mechanical phasing to ensure links are vertical / not binding)
- Pitch Pump booster: Unchecked
- Signal Processing Extended: Unchecked
Here's a picture of the setup in the helicopter:
I'm really hoping that someone can help here. These fuselages are next to impossible to find, and I would be heartbroken if I stuffed it in.
This is a matter of national Czech pride... Because this is what he'll look like when done!
Yup... That's 7353, who is part of the Czech Air Force, in Namest as part of 221.lbvr. He's won best livery at the international Tiger Meet.
Thanks for the help!
cheers,
ed