Hi,
I have the problem that if I connect the Jive Telemetry cable I cannot fly as the Spirit Pro shows erratic behaviour on all axis like with static electricity. I optimised the cables but it does not change anything.
I still done the following before disconnecting the Jive Telemetry cable.
- exchanged the motor
- optimised cables
- added a ferrit ring
- grounded the tail
Nothing changed the behaviour only disconnecting the Jive telemetry helps. So what could be wrong? It happens in flight only so without mainblades everything is fine. Perhaps I should move to a Jlog to get Jive away from the satellite ports? Or any other advises?
Using firmware 2.8.
Cheers,
Nils