ZeXx86 wrote:
Hi,
it is very likely that improper CG is causing this.
You can move battery just temporarily to see how the behavior will change.
Sometimes when moving with collective pitch up and down one of the servos are moving unequally. This then could cause the behavior as well.
Or one servo is slower than other due to a friction or other mechanical issue.
You could verify (ideally with a Cyclic Leveler) that the the swashplate is really level also at the low and high pitch position. In case it is unequal you can fix it with the Servo Travel Correction. You can find it in the Servos tab.
Hopefully this will help you.
Thanks Tomáš. I moved the pack as far forward as the canopy allows and while it’s still not perfect, the pitching issue was pretty much non existent. I think that solved it.
I think I kept moving rearward trying to solve the pitch issue and kept making it worse despite it being counterintuitive.
Thanks!
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