It is currently Sat 23. Nov 2024 12:22:37

All times are UTC + 1 hour





Post new topic Reply to topic  [ 7 posts ] 
  Print view Previous topic | Next topic 
Author Message
PostPosted: Sun 20. Mar 2016 7:03:26 
Offline

Joined: Fri 03. Apr 2015 2:31:10
Posts: 10
My Oxy 3 had been flying well. After updating Spirit from v1.3.2 to v2, I have fast tail wag even during hovering. At the same time, I have also changed my motor pinion from 11T to 10T.

My Oxy 3 setup:
- Main blades 285mm
- Tail blades 47mm (13T)
- Motor Lynx EOX2214 v2 (4100kv)
- Talon 35 (governed at 3,500 rpm)
- Cyclic & tail servos Turnigy S306G HV
- Battery 4S
- Main gear 140T
- motor pinion 10T
- Pitch 12 degree
- Cyclic 10.5 degree

I have disabled the governor in Talon and ran a 95% flat throttle curve and lowered the rudder gain all the way from 50 to 35 and the tail wag is still there.

The tail wag is bad especially in fast forward and fast collective change.

Can help me take a quick look at my settings to see whether there is anything obviously wrong?

Cheers
Peter


Attachments:
File comment: v2 setting
Spirit 20160316-0.4ds [255 Bytes]
Downloaded 46 times
File comment: v1.3.2 setting
Spirit 20151117.4ds [255 Bytes]
Downloaded 45 times
Spirit settings.pdf [32.16 KiB]
Downloaded 62 times
Top
 Profile  
 
PostPosted: Sun 20. Mar 2016 7:14:12 
Offline
User avatar

Joined: Sun 26. Jul 2015 8:17:50
Posts: 433
Location: Madrid, Spain / Torino, Italy
Well, changing your pinion you slowed down your mains, so something also changed there...

Is it a fast wag like shaking or more a hunting where the tail does not react fast enough so it overdoes?

In the second case you should be raising your tail gain, it looks like you only tried to lower it.

_________________
Oxy 2X-VertWarp 360Blade 450XBlade 450X NightflyerGoblin 500 (RIP) ♦ 2 X mCPX v2 ♦ night fly mQXLadyMQXnano QXnano QX FPVInductrixDX8 G1


Top
 Profile  
 
PostPosted: Sun 20. Mar 2016 7:33:22 
Offline
User avatar

Joined: Fri 05. Feb 2016 21:03:44
Posts: 30
My Oxy is also running 4s but with castle simple gov. I'm running 12t at 3800. And Spektrum h3050/60.


The pin size should be ok for 3500 so I don't think that's an issue. What are your vibration logs showing maybe your motor is resonating at that HS


Sent from my iPhone using Tapatalk


Top
 Profile  
 
PostPosted: Sun 20. Mar 2016 9:44:53 
Offline

Joined: Fri 03. Apr 2015 2:31:10
Posts: 10
The wag is 3 to 4 hz.

I did not check the vibration log. Apart from a bit of resonant vibration at about 3000 rpm, it seems to be alright.


Sent from my iPhone using Tapatalk


Top
 Profile  
 
PostPosted: Sun 20. Mar 2016 10:36:45 
Offline
User avatar

Joined: Sun 26. Jul 2015 8:17:50
Posts: 433
Location: Madrid, Spain / Torino, Italy
phwm wrote:
The wag is 3 to 4 hz.

I did not check the vibration log. Apart from a bit of resonant vibration at about 3000 rpm, it seems to be alright.


Sent from my iPhone using Tapatalk


No idea what you mean with "3 to 4 hz", sorry.

_________________
Oxy 2X-VertWarp 360Blade 450XBlade 450X NightflyerGoblin 500 (RIP) ♦ 2 X mCPX v2 ♦ night fly mQXLadyMQXnano QXnano QX FPVInductrixDX8 G1


Top
 Profile  
 
PostPosted: Sun 20. Mar 2016 13:29:05 
Offline
Site Admin

Joined: Mon 29. Apr 2013 16:06:44
Posts: 12442
What is wrong in the settings is Rudder Delay and possibly Pirouette Consistency.
But the settings should be same for new and old version.

For your tail servo the Rudder Delay should be between 0 - 5 and Pirouette Consistency 170. Rudder Delay should help with your problem significantly. Did you used these values previously too?

Changing pinion will affect many things, but if you will reach same head speed, then it should work in the same way theoretically.
In case that you are flying with the same head speed, it is probable that because of higher motor RPM you are getting some very bad vibrations from the motor that were not present with a bigger pinion.

_________________
Spirit System developer


Top
 Profile  
 
PostPosted: Sun 20. Mar 2016 14:36:24 
Offline

Joined: Fri 03. Apr 2015 2:31:10
Posts: 10
The tail wags to left, returns to center, then to right and returns to center in about half a second.

I have been using default for 450 and have not changed the system values for tail delay and piro consistency.

Now back home did a spectrum analysis. X and Z axes seemed to be fine. However, vibration in the Y-axis (aileron) was bad. If I disengaged the motor pinion from the main gear, there was totally no spike of vibration.

If elevator was fine but not the aileron, then I guess it cannot be the bearing block.

Which part should I test next?


Attachments:
z.png
z.png [ 41.95 KiB | Viewed 877 times ]
y.png
y.png [ 36.53 KiB | Viewed 877 times ]
x.png
x.png [ 23.67 KiB | Viewed 877 times ]
Top
 Profile  
 
Display posts from previous:  Sort by  
Post new topic Reply to topic  [ 7 posts ] 

All times are UTC + 1 hour


Who is online

Users browsing this forum: No registered users and 44 guests


You cannot post new topics in this forum
You cannot reply to topics in this forum
You cannot edit your posts in this forum
You cannot delete your posts in this forum
You cannot post attachments in this forum

Search for:
Jump to:  



Powered by phpBB © 2000, 2002, 2005, 2007 phpBB Group
skymiles_red v1.0.1 designed by Team -Programming forum-سيارات للبيع .