Hi, used the gov for the first time on the nitro today ( Trex 600 - YS 60SR - Align sensor). Still in the break-in cycle on this engine, so gentle flying and low headspeeds.
Observation so far is an intermittent problem when going down in headspeeds, from IU2 to IU1. Switching up doesn't seem to have any problems. Throttle curves are set to only change a few hundred RPM between each. When switching from IU2 back down to IU1, the gov closes the throttle completely and then opens it up again. It almost seems as if the headspeed doesn't drop fast enough for the gov, so it keeps closing the throttle. When it does slow down, it drops too low and then the gov yanks it open again. Gov settings are 3 & 2 at present.
A few times, I landed, idled for a while (more than 10 sec) and then tried to take off again. At which point the gov wouldn't engage. Shut it down, cycle the power, start up and all is fine again.
I will start leaning the engine out during the next flight session and will also then test different gov settings.
All while we're waiting in great anticipation for 1.3 ...............